Life
as a Blown V6
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May 2003
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May
31st
First official day of reconstruction. FMU and In-Line Fuel pump
successfully connected. Bracket and Blower test fit as well as some
ducting. Adjustments made as seen fit. Thanks to Gangreen,
PJ, and Turbo-Benz things went pretty well. |
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June 2003
June
1st
PJ was kind enough to help with constructing intercooler straps
so the J-bent-pipe will fit above the intercooler. Unfortunately,
the thing is now pretty much as the same level as the bottom of
my front tires. Work continues. Otherwise, Blower ducting completed.
Fuel pump and relay mounting holes drilled. Everything seems bolted
up. Blower belt extremely tight but on. |
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June
2nd
Relocated intercooler. Started the car. Stefan drove it up the road
and back down to its parking spot. Blower belt fragmented -
belt size 42.75" too small. Moving up to 43.5". Left headlight
no longer raising, motor does not appear to be receiving power. |
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June
3rd
Pathogen driven NA for state inspection. FMU vacuum source not connected.
Tool needed to remove square from near back of intake. Testing continues. |
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June
4th-6th
Intercooler and ducting relocations continue. |
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June
7th
Attempted to drive Pathogen to the monthly HideOut
gathering. Made it 4 miles before the Blower shifted and pulleys
began to rub together. Testing continues. |
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June
10th
Tool for removal of square purchased and sized - piece removed.
Mounting Point C doesn't seem to fit correctly. Testing continues.
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June
11th
Intercooler relocation continues. Replacement piece found for intake.
FMU vacuum source connected.
(Down time taken to allow swelling to go down. No one sells gloves
for people with small hands!) |
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June 14th
Shimmed Bracket to keep pulleys from running together. C mounting
point is in, but won't thread. Testing continues.
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June
15th
Intercooler Relocated to work with included straps. No longer need
to cut-up 2 180` bends, just need one now and a rubber 90` from
Lowes. |
June
16th
Shredded second belt. Shimming bracket resulted in belt rubbing
against the bracket. Distance: 4miles. Testing continues. |
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June
17th
Pathogen completes a 10 mile round trip to work and back with no
belt wear. Testing continues. |
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June
18th
Pathogen does it again. Testing continues. |
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June
19th
Car pool to work, Virus shorts out in the rain.
Pathogen makes the round trip for tools. Still no belt wear. Testing
continues. |
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June 20th
Pathogen makes it to 50 miles blown and arrives at a local car
hang out. Notice take of old belt pieces between Charger and Charger
pulley. Small bit of oil on Throttle body and back-side of Charger.
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June
21th
Pathogen shuts down on way to BK HideOut
gathering by way of a massive oil leak. Car is nursed to a nearby
Sheetz where the Charger is removed. No source of oil leak found.
Oil lines are capped. Car driven home NA. (total fluid loss - 1qt.)
Testing continues. |
June
22nd
Repairs. New return line built and installed. Charger reinstalled.
No oil in the ducting so Charger doesn't appear damaged. Seal in
high-pressure oil feed line appears to be broken. 'Band-Aid' constructed.
Line is under heavy watch for further leakage. Replacement from
ATI or other source is expected. Testing continues. |
June
24 AM
Pathogen makes it to work blown, but is constantly stalling every
time I let off the throttle. Bandaid seems to have failed, allowing
oil to leak from the charger-end of the high-pressure oil feed line.
Pressure: 65ish at 2G.
I'm beginning to wonder if there's something clogging the charger's
oil-pressure nozzle, creating un-goddly pressure inside that line.
While at 2G or higher, the oil pressure increase is enough to over
come the loss from the leak. Otherwise it's low; do these cars shut
down automatically if a sensor says "you're running dangerously
low oil pressure"? (I was watching my tach, and not my oil
gauge while trying to keep the car running.) That would also make
the bandaged fail. |
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June
24 PM
Path makes it back with no problems. Running a bit uneven, but not
stalling. Pressure seems normal. No 'fresh' oil in engine bay, no
belt wear. Testing continues . . . |
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June
25
Oil leak reappears. Source believed to be a bad feed line. |
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June
26
New feed oil line constructed and installed. Test drive to be conducted
in the morning. |
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June
27
Oil leak still present. Now I'm completely baffled but have narrowed
the possibilities of the problem. Car put down for repairs and further
observation. |
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June 28
After a 15 minute observation period, source of the oil leak has
been found. Car runs "normal" up to 3000RPM with no
oil leakage. At 3000, oil literally pours from the pulley side
of the Blower. Charger scheduled to be rebuilt by ATI ProCharger
shortly. Standby for future updates.
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July 2003
July
01
Contacted ATI regarding rebuild of the Blower. Got RA#. |
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July
02
Mailed FedEx Ground to Kansas
for repairs. |
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July 08
Blower arrives in Kansas for repairs.
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July
11
Received phone call from James at ATI ProCharger. (A game of phone-tag
ensues). |
July
22
Contact is made. Blower front seal repaired under warranty.
Outer housing rotated a few degrees south to about 5 o'clock.
Possibilities for the blown seal are discussed. Current ducting
setup to be looked over.
Blower scheduled to return July 25th. |
July
25
Blower arrives from ATI. ProCharger bolted on and oil lines connected.
Round trip of 30 miles showed oil leak from return line. |
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July
26
Belt connected, new air ducting connected. Oil leak still present.
Round trip of 50 miles showed oil leak from return line at oil pan
and belt walk. C-mounting point seems to be stripped in the block
- have to fix that. Shims on A-mounting point seem to be setting
the belt off to the front of the block and causing belt walk. "Firestorm"
graphics finally applied. (Thanks to Firebat's Cave to helping with
these!) |
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July
27
Fell asleep under car. Fixed oil leak. All seems almost right with
the world. |
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August 2003
August
1
Removed sims on A-point to straighten belt. Tighted B-point before
connecting to Blower seems to have strengthened the positioning
of the Blower. Still working on getting that C-point to thread,
I've finally come to the conclusion that the hole is stripped. |
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August
2
Completed ducting by making temporary fix for the inlet as that
orange hose has successfully shredded to pieces. Tied oil return
line away from damaging belts and pulleys.
New TO-DO-LIST
as directed by
members of the F-Body Hide
Out.
1). Re-run return oil line to fix tiny-little oil leak
2). Re-locate Adjustable tentioner on Blower bracket
3). Complete Outlet ducting. (plumbing, blow-off valve relocation)
4). Re-run Inlet ducting using drier-hose and allowing for whisper
lid
5). Seal C-mounting point to stop coolant loss. |
August
11, 2003
Now fitted with BF Goodwrench Drag Radials, Pathogen hits the road
again. Few problems remain. Inlet ducting still needs to be replaced,
and the C-mounting point needs to be fixed. Running is smooth and
consistent. |
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August
14, 2003
Blower removed to complete adjustments in preparation
of the F-Body Nationals in Englishtown, NJ on August 16th. Ducting
is rerouted, C-mounting point replaced by a stud, return oil line
replaced. While reinstalling the Blower, something cracked resulting
in massive coolant loss. Trip to Nationals canceled. |
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August
16, 2003
Search for the mysterious coolant leak begins with the non-fuctional
AC delete. Blower removed. On a whim, I removed the Radiator
cap to check the coolant level, thus allowing air into the system
and breathing life back into the leak. Source of leak found to be
in behind mounting point-B - Timing Cover. Removal of Crankshaft
pulley will be required and I lack tools for the job. Negotiations
with local garages and tow companies begins in the morning. |
August
28, 2003
Good news! Notice received that a garage unit closer to our apartment
is opening up (Unit #7). Our current/soon to be old unit (#16) is
on the opposite end of the complex. Bad news; unit #16 needs to
be empty on 8/31/03. |
August
29, 2003
Water pump removed and AC delete completed. |
August
30, 2003
Pathogen is pushed from the garage into a neighboring spot and covered. |
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August 31, 2003
Garage transfer completed. While in transition, I over heard something
resembling an air-wrench from in side a garage. After explaining
the problem and discussing the cost of towing a car, access to
an air-wrench and a very willing assistant is achieved.
Pathogen is pushed to Ray's Garage (Unti
#10) where the Crankshaft Pulley bolt finally removed.
Pathogen is then pushed to a spot directly in front of the rental
office.
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September 2003
September
3, 2003
General Tear Down Continue. Pulley puller not working with the crank
pulley |
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September
5, 2003
New Timing Cover Arrives. Crankshaft Pulley finally removed with
a second pulley puller. |
September
6, 2003
Reconstruction Continues. Oil-pump not lining up with crankshaft. |
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September
7, 2003
Timing Cover installed. Path refuses to start. |
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September
9, 2003
CPS replaced. Path moves 50-feet under his own power and no serpentine
belt. |
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September
10, 2003
Pathogen returns to the road for a 10-mile test drive; NA and no
AC. 61" belt used. Repeated stalls while downshifting assumed
to be driver-error. |
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September
11, 2003
Pathogen attends the Ride for Pride 2003, Pentagon memorial cruise
along the George Washington Memorial Hwy with the F-Body
Hide Out and CrossRoadOnline.
No leaks, no stalling, no overheating, and no Blower. Headlight
damaged on June 2nd begins working at the Pentagon.
(Pictures thanks to CrossRoadOnline)
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September
14, 2003
Massive Detailing project continues over from the 13th. Bracket
test-fitting begins. B-point is not sitting flush on the timing
cover. Modifications made (via file). C-point (extended do to missing
AC bracket) appears a bit too short, causing the bracket to bend
in-ward on the bottom.
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September
21, 2003
Blower reinstalled. All bolts tightened, including C! Oil lines
connected with new routing. Spark plug wires replaced - two of six
sparkplugs replaced (grumble). Waiting on gaudy-orange silicon hose
replacement from ATI. |
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September
27, 2003
Two sparkplugs replaced in the morning, gaudy-orange silicon hose
and remaining ducting installed. Battery box acquired (car needed
a jump). Gangreen swapped
the last two plugs in the afternoon, gave the car a once over and
found a coolant leak.
Note made that the stock radiator-mount-panel no longer fits (do
to AC-delete). Replacement to be acquired. Leak is being repaired. |
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September
30, 2003
Pathogen returns to the road. |
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October 2003
October
1, 2003
Well, good news - we've got boost! Unfortunately, that news was
announced when I shot my dipstick on the drive home from work leaving
those behind me gasping in a cloud of blue smoke. |
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October
2, 2003
Just to see how things would hold up, Pathogen makes a trip to the
local 8th to see if any improvement was made. The car holds together
to show a 2-tenths 1/8-mile improvement and a 3-mph improvement. |
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October
4, 2003
Pathogen arrives at the monthly F-Body
Hide Out gathering Big, Bad, and Blown. And, not to disappoint
anyone, catches fire on an exhaust manifold right below the FMU.
No damage resulted, but concern mounts with regard to the up-coming
trip to NJ. |
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October
10, 2003
Minor repairs are made from under Gonzo's
trailer at the Ramada (Official lodging location of the F-Body
HideOut). Ducting issues were brought up and a oil leak was
fixed. |
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October
11, 2003
Pathogen runs at Englishtown, NJ with serious mechanical difficulties.
Times are not being disclosed at this time. |
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October
18, 2003
Using an K&N Breather for a Mustang, and a spare oil-fill cap,
a breather is fabricated. Initial tests show signs of oil leaking
from breather at boost, but nothing as bad as blowing the dipstick. |
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October
23, 2003
Pathogen runs at Summerduck
Dragway, VA. New bests for the 1/8th -- 9.455 @ 77.12, with
a 2.240 60'. |
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November 2003
November
27, 2003
160-Thermo installed. On test drive, Pathogen catches fire again.
No visible damage.
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December 2003
December
10, 2003
RK Sport headers arrive, install to begin sometime-or-other. |
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December
28, 2003
Coolant leak solved. A plastic elbow had broken inside the alternator
bracket. Attempt made to fix on going 'belt squeak' issue. Crank
shaft pulley was removed and reset. Squeak returned during a short
test drive. Oil leak from feed line remains. Hopefully this squeak
is related to oil getting on the belt. (Squeak goes away after car
has been on the road for a few miles.)
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